Yep the dipstick was too short but it didn't cause the stuck ring,low #4 compression or a injector to not fire. Even with a metered 5.5 quarts of oil the crankcase was still getting blow-by. And #4 is still not fueling,I hope to work on it in a few days.
I did run the engine a quart over full and resulted in a slow to rev engine and hopefully no internal damage. I was assured it was the correct dipstick early on in this daboggle.