The turbo motor lost a piston, ground up the
oil pump, ate the #1 rod bearing, and I think
broke the crankshaft while driving home from Moab

I'm going to put it together in N/A form, go get my
smog check and then redo the turbo on a 16V head
and go all MegaSquirt, including Ign control/boost retard
So if you want to get some testing in while I'm in the
transitional stage of N/A to Turbo, I would go do some
measured 1/4s and see what happens
Wild